03/07/20 Fri.  My diaphragm arrived yesterday afternoon, two 
		and a half days behind schedule so not bad.  Today, I stripped down 
		the pneumatic governor, removed the old diaphragm (which had a split in 
		it) and replaced it with the new one.  The engine now revs at a 
		more manageable speed.  However, the overheating problem still 
		remains, in fact it's worse now and we were up in the 90's just 15 mins 
		after running the engine at 800rpm.  Tomorrow will be a long day of 
		checking everything possible.
		
        04/07/20 Sat.  On checking the water level this morning, it 
		was down considerably.  I topped it up again and fired up the 
		engine.  It ran fine for an hour at idle revs, not going above 65oC, 
		then I put it in gear to load the engine and upped the revs to 1400, ran 
		it for a half hour and it stayed at 74oC.  
		I don't think the thermostat opens until 78/79oC 
		so it looks like it is just difficult to fill from totally empty due to 
		airlocks.  I will do a bit more to it before being satisfied!
		
        06/07/20 Mon.  I had my haircut yesterday, it was driving me 
		nuts touching my ears!  We walked up to the garage this morning at 
		6.30am and got some more diesel, petrol and ATF oil for the gearbox.  
		During the afternoon, I drained the engine cooling jacket again and also 
		the gearbox oil - which I then replaced with the new ATF.  I have 
		put one or two photos on my 'workshop' page regarding the change of 
		governor diaphragm which you can see 
		here should you be interested!
        07/07/20 Tues.  Time for another moan!  My elapsed time 
		from Gillingham count-up timer is no longer working as you can see 
		below.  This is because Microsoft, in their infinite wisdom, have 
		disabled javascript for their Edge browser.  If you have the 
		Windows 10 Pro version it is possible to enable scripts again, but for 
		me with the Home version, it is impossible.  Why do Microsoft have 
		to be so bloody awkward!!  I can't find any other way of making a 
		timer, it isn't possible with HTML code, so unless someone lets me know 
		of a way to write a new script, I will have to delete the one at the 
		foot of the page.
        09/07/20 Thurs.  OK, a bit of a mishap yesterday morning,
 we 
		were walking to the garage again to get another 20 litres of diesel.  
		My right foot slipped on a wet patch of slime across the pontoon and my 
		following (left) foot automatically came down fast to stop the slide.  
		It came down mid step and toes first - and crashed into the concrete, 
		making me say a few choice words.  I should have gone back to the 
		boat immediately and put it in cold water, but we continued to the 
		garage and back with the diesel.  That afternoon and evening were 
		absolute agony!  I didn't get any sleep last night, and today I 
		have a big toe 75% bigger than it's opposite number, the nail is cracked 
		and the toe is rainbow coloured.  The rest of my foot is also 
		swollen.  So, today I didn't do anything except sit and read!
        11/07/20 Sat.  My toe is much better now, not hurting nearly 
		so much.  I can't really walk or wear flip flops just yet, but I 
		can get around the boat!  We lifted the dinghy up on deck this 
		morning - it's been in the water since pushing the boat over to A Dock 
		two weeks back, was full of water from the daily rains and the bottom 
		needed a good wash to remove marina dirt and barnacles.
        16/07/20 Thurs.  After two and a half days with no water, it 
		was finally reconnected this morning - takes a long time to fix a simple 
		plastic pipe leak here!  B Dock still has no electricity, that's 3 
		weeks now.  We are now looking at leaving and heading up to Kudat, 
		the visa problem is a worry but I guess it will all work out in the end.  
		We went into town this morning and started to stock up with canned food, 
		fresh chicken and veg in preparation for leaving.  As I type this, 
		a terrific storm is raging, thunder, lightning, torrential rain and 30 
		knots of wind from the East - which of course is the way we initially 
		have to go!
        21/07/20 Tues.  We did plan to check out today and sail in 
		the morning but Ana was feeling a little off colour today (nothing 
		serious) so we decided to postpone for a day.  The weather is 
		fairly stable at the moment but we still have nightly rainstorms.
        22/07/20 Weds.  Checked out today with all the relevant 
		authorities and we will sail tomorrow morning about 0600.
        23/07/20 Thurs.  Slipped at 0700 and made our way northwards 
		to Pulau Tiga.  On approach, the wind picked up to 30 knots which 
		would have made our anchorage on the south side of the island far too 
		exposed, so we turned to starboard and anchored in about 10 metres in 
		the lee of Kuala Penyu headland.  Around 4pm, a terrific 
		thunderstorm rolled in right over the top of us, sending multiple bolts 
		of lightning down around the boat (maybe 200 feet away) - extremely 
		scary and I was convinced we would be hit by one!  All was well 
		though and after an hour or so, it passed over us.
        24/07/20 Fri. Weighed anchor at 0500 and continued northwards to 
		Teluk Usukan (with an option of Pulau Dinawan if the weather got bad.)  
		6 miles short of Usukan, the heavens opened and we had a serious 
		downpour.  It was 3pm and we had navigation lights and steaming 
		lights on, visibility was almost nil all the way into the bay and 
		standing at the bow dropping the anchor in pouring rain is not much fun!
        25/07/20 Sat.  This morning, I am full of a cold!!  Day 
		of rest, the bay is calm, almost zero wind, clean water and the resident 
		turtle swimming around - can't be bad.
        26/07/20 Sun.  We decided to stay another day relaxing.
        27/07/20 Mon.  Today's plan was to head 30 or so miles 
		further north and anchor in Teluk Agal because winds were forecast to be 
		favourable for that particular anchorage.  I've anchored there 
		several times before, and aborted once before because the waves roll in 
		and break on nearing the beach if from the SW.  10 miles out, it 
		was obvious that we were out of luck with the wind, so we altered course 
		and headed for the tip of Borneo, rounding it at 1500.  Then it was 
		just a couple of hours down to Kudat.  Something seemed not right 
		with the steering, it was becoming vague and I could hear a 'clonking' 
		noise sometimes.  We were too tired to bother with inflating the 
		dinghy and readying stern lines to moor in the pond, so we continued 
		past Kudat Pond and anchored in the bay off the town.
        28/07/20 Tues.  Weighed anchor at 0630 and motored around to 
		Kudat Pond.  We had arranged to pick up Neil (Shelley) from 
		Penuwasa to help us with the mooring and it was a good job we had!  
		On entering the pond, we experienced a total steering failure!  So 
		my suspicion of a problem yesterday was correct.  Things could have 
		been worse of course, it could have failed anywhere on the journey, 
		especially rounding the tip of Borneo.  We used the boat engine to 
		push us forward while Neil pushed my bow with the dinghy to steer and 
		picked up Neil's vacant mooring lines.  A quick look then at the 
		steering, and the fault is obviously inside the steering pedestal which 
		is going to be a real problem to a) take apart, and b) to get spares 
		for.
        29/07/20 Weds.  Neil came over to give me a hand with the 
		steering problem today.  First we took off the lower gear box which 
		wasn't driving the torsional rotation output bar and we immediately 
		noticed the 'male' splines on the vertical shaft were worn as well as 
		the bearings in the gearbox.  The 'female' part of the splines are 
		up inside the pedestal and initially inaccessible without further 
		dismantling.  Having no diagrams or drawings of the assembly  
		to study made it all a matter of engineering logic and 'feeling' our 
		way.  Day one over.
        30/07/20 Thurs.  We need to remove the long vertical shaft 
		from the pedestal and I was told by a member of the Warrior Facebook 
		page, that it had to be removed from the top of the pedestal, which is 
		understandable because there is insufficient room to withdraw it 
		downwards into the engine bay.  First we had to remove the steering 
		input shaft which runs horizontally across the top of the downward 
		shaft.  This proved a real challenge as the 'bearing' socket for 
		the shaft had been sealed in by some previous owner.  We used three 
		kettles of boiling water to expand the head of the pedestal as much as 
		possible and drifted the socket out - it's cast alloy, and unfortunately 
		two pieces of it broke off.  I will have to see if that can be 
		repaired further into the job.  Day two over.
        31/07/20 Fri.  Again we used hot water to expand the 
		vertical shaft bearing carrier and at the same time, drifted the shaft 
		out from the bottom of the pedestal.  It only came part way! There 
		are two bearings holding the shaft at the top and there is absolutely no 
		way to remove the second bearing.  Now we had little choice but to 
		unbolt the seven deck bolts holding the pedestal to the deck and remove 
		the whole thing.  Once that was out, we brought the shaft up again 
		and removed the top bearing, circlips and keyway, then we could withdraw 
		the shaft downwards again, leaving the second bearing at the top of the 
		pedestal.  Just how you are supposed to change that I have no idea, 
		it would have to come downwards and it's at the end of a 30" tube that 
		is 4" in diameter and no way to get to it!  Now we had the shaft 
		out, it was plain to see that the 'female' splines were also stripped 
		out.  So now it's all apart and I know what has to be repaired.  
		It will be a long job that's for sure.  Three days to strip it out. 
		
		
	
		
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