01/11/11 The problems continue!
This morning when I put on the nuts of the flexible coupling, they
jammed against the back of the gearbox and prevented the prop shaft from
moving more than a quarter turn in either direction. After
struggling for some time, I decided it would have to come off and be
inspected......but I couldn't turn it to get at the lower bolts!
Hours passed before I had the coupling in the cockpit, and thinking of
when I fitted it in Langkawi with no problem made me realise that it
must be I that had made some elementary mistake. Close examination
of the eight bolts revealed that four of the eight are fractionally
shorter than the others, and two of the shorter ones had been
interchanged with two of the longer causing the jamming. Once I
had got all the bolts in the right holes, the coupling went in and was
tightened up with relative ease. Tomorrow comes the contortionist
act with the feeler gauges to check clearances on the coupling top,
bottom and sides.....the difference between minimum and maximum gap has
to be less than 0.25mm.
02/11/11 By about 2pm I had the engine
as lined up as I was ever going to get it (difference 0.20mm) and bolted
down the mountings. After reconnecting the exhaust pipe, gearbox
linkage and throttle cable it was time to give the engine a try and true
to form......another problem raised it's ugly head. On starting,
the alternator warning light and buzzer remained on and the
ammeter showed zero. OK, I've dislodged a wire somewhere on the
charging circuit and tomorrow I will find it.
03/11/11 Spent the whole day checking
out the cable runs to and from the alternator. I took down the nav
berth wall and checked the master switch connections, the battery
connections and anything else I could think of - but the problem
persists. I can now only think that the alternator itself has
failed internally, but why would that happen while it was not in use?
04/11/11 I took off the alternator and
Stefan ran me into Gadong to an alternator test shop. A bench test
showed it to be OK.....so that eliminates that! Other yotties
suggested the ammeter may be at fault, or the split diode on the
charging system, so that's the next thing to do - bridge the terminals
and see if that cures the problem.
05/11/11 Went over to Barry's boat
(Fourth Dimension) to give him a hand with his mainsail halyard
which had come adrift and was trapped at the top of the mast, but high
winds and rain prevented us doing the job - so we had a few beers
instead.
06/11/11 This morning I replaced the
alternator but before stripping out the nav. berth again to get to the
back of the ammeter, I decided to just start the engine and see what
happens. The fault had disappeared!! Now I can only believe
that the earth strap from the alternator to the engine block was somehow
at fault - although it isn't very old. Anyway, the engine doesn't
seem to be giving out vibration as badly as it was, and the prop shaft
speeds up when the revs are increased. However, there isn't the
normal 'wash' created at the stern when the engine is revved to 1500rpm.
It's probably due to barnacle growth on the propeller if the anchor
chain is anything to go by. I hauled up 10 metres of anchor chain
and knocked off the barnacles with a welder's hammer. Again went
over to Barry's boat and this time was able to ascend the mast and free
his halyard. BBQ onboard Storm Dodger in the evening with
Paul, Alison, Barry, Sue, Stefan, Lorna and others, slightly spoiled by
high winds and rain.
07/11/11 A day of tidying up the boat,
cleaning the log impeller and shower tray filters. Rog came over
to dive and clean off the barnacles on the propeller and we went over to the
Customs, Harbourmaster and Immigration to check out for tomorrow.
Looking at my last November log shows a remarkable similarity to this
log.......climbing other peoples mast, fitting shaft couplings and
engine mountings!!
08/11/11 Helped Roger with his dinghy
repairs and barnacle cleaning. Lashed down the new jerry cans
before going ashore again to meet up with Stefan and Lorna for a
farewell drink. I've now opened another page to show the gearbox
change here.
09/11/11 Our intended departure today
has been postponed because of the additional jobs (Roger's dinghy and
various other bits and pieces). We WILL try and leave tomorrow!
10/11/11 Best laid plans and all that.
An unexpected squall arrived this morning, bringing 30 knot winds and
heavy rain which lasted until mid-day - our intended departure time.
Thoughts of what lay outside the harbour made us decide to stay
overnight and leave early in the morning.
So this would be our last Muara sunset!
11/11/11 Weighed anchor at 0630 and made
my way down the harbour behind Storm Dodger, clearing the
approach channel by 0800 (slowly against the flood tide). The
crossing to Labuan was fairly uneventful although I worried a lot about
the stern gland and kept a close watch on any water drips from that
area. My speed impeller was not working despite being withdrawn
and cleaned just the other day and although I cleaned and checked it a
further twice during the trip, it was still showing zero knots on our
arrival in Victoria Harbour. It was easy to observe more than two
minutes silence on this notable Remembrance Date prior to my arrival at
the harbour entrance. The harbour is renown for bad holding due to
the amount of rubbish (plastic bags etc) on the seabed but I was lucky
and the anchor dug in on the first attempt. Shortly after we
arrived, Barry on Fourth Dimension motored into the anchorage on
his usual Friday expedition to Labuan and we later saw him in Murphy's
Irish Bar before he headed off back to Muara. We cleared in with
Custom's but the Immigration and Harbourmaster were closed for lunch -
and we missed their one hour of opening in the afternoon! During
the evening, a squall hit the anchorage and although the winds only got
to 28 knots, the waves caused the boat to pitch like a wild horse for a
couple of hours. I turned on all instruments and ran the engine
for an hour until the worst had passed and I was sure the anchor was
holding firmly.
12/11/11 I again cleaned the speed
impeller and left it withdrawn, I must remember to replace it just
before leaving again! I also decided to check the three stopcocks
in the same bilge - the first (to the watermaker) was fine but the
discharge and inlet (traditional Blakes valves) to the head were both
seized so I would need to free them off. I slackened the keeper
plates and gingerly tapped the handles with a mallet until they both
began to turn. When I tightened the keeper plates, the inlet valve
continued to leak water into the boat! It really needed to be
ground with carborundum paste but I would just have to re-grease it for
now. It's always a nerve jangling moment when you remove a valve
and the water floods into the boat! I bunged the hole with a
wooden plug while I cleaned and greased the tapered valve, then replaced
it in it's sleeve - temporary repair done. I then went ashore to
the Harbourmaster's office but again it was closed and will not re-open
until Monday.
13/11/11 Happy
Birthday David! Remembrance Sunday......and the
first time I've worn socks and shoes, with long trousers for a
considerable time! We went to the Labuan World
War II Memorial at Jalan Tanjung Batu for the Remembrance Service, where 3,908 Allied
soldiers, sailors and airmen are buried. The service was attended
by local dignitaries, the UK deputy commissioner for Labuan, serving RAF
personnel, Malay Armed Forces and ex-service personnel from the UK,
Australia, New Zealand, India and Malaysia. As all were wearing
their medals, it was a shame that mine are in the UK - in fact this was
the first time I've had sight of the Pingat Jasa Malaysia medal (which I
received only last year). Click the image
on the right for some photographs. On completion of the service, we made
our way back into town and had some lunch in Murphy's Bar while watching
the welterweight boxing championship before returning to the boats for
another rolly evening! The relief in taking off my shoes was
immense for I now had burst blisters on my left foot which were killing
me!
14/11/11 Into town again, this time to
the Harbourmaster to check in and check out in readiness for leaving
tomorrow, weather permitting. Also did some shopping for
essentials and had dinner in Murphy's.
15/11/11 I was up for a great deal of
the night, coughing, sneezing and completely 'bunged up.' I had
felt a sore throat coming on for the last 24 hours and knew I would be
coming down with the proverbial 'man flu.' As Jordan on Storm
Dodger was also suffering the same ailment, we decided to wait until
tomorrow before sailing.
16/11/11 Weighed anchor at 0715 and made
my way slowly out of the harbour while waiting for Roger to fix an
electronic problem on his chartplotter. We then set course for
Pulau Tiga with a favourable, if gentle wind which allowed me to use the
genoa for a while. With the watermaker running, I put 90 litres
into the tank and dhobied a few t-shirts en-route. Storm Dodger
caught a barracuda weighing 8kg and measuring a metre in length but I
hadn't bothered to trail a line on this trip. We arrived at the
anchorage about 4pm and dropped the hook in five metres of water, laying
out 30 metres of chain before going ashore to have a look around.
The island is more popularly known as 'Survivor Island' because it's the
site used for filming the television reality series 'Survivor.'
There is a small resort of chalets but on our visit there were no
guests! Roger asked the chef if he would cook the barracuda for
us, which he did and we all enjoyed huge plates of the fish done in
batter and soy sauce......I hope none of us now have ciguatera
poisoning!! During the night, the anchorage was very rolly and
electric storms could be seen all around us.
17/11/11 Our plan to leave this morning
was again changed and we decided to trek over a kilometre inland, up a
steep and slippery jungle path to see the mud volcano, where we
'wallowed' for an hour. It was impossible to sink into the
bubbling, thick glutinous mud, even if you tried to push yourself down
on the ropes strung over the pit. When we got out, we found there
was no way of washing off except for a very low rainwater supplied tap
under which you had to crouch! So, we trekked back down to the
beach, slipping and sliding most of the way (flip-flops were not the
ideal footwear!), and went straight into the
sea to clean up a bit. (some photo's) Later on, Roger got his diving gear out and
he and Astrid again cleaned both boat's bottoms as progress here had
proved slow.
18/11/11 Weighed anchor at 0715 and made
our way around the eastern end of the island before setting a course
toward Mount Kinabalu, it's high summit visible in the distance.
Because of a fairly constant light breeze, this was one of the most
enjoyable motor sails I have had in recent months - and I caught
a nice 30 inch Spanish Mackerel! But in the last five miles, things again started to go wrong
again, the engine started losing revs and giving more throttle didn't
make any difference. An inspection revealed that the water
injection elbow on the exhaust system had been holed, probably as a
result of chemical reaction between combustion products and sea water,
and the engine bay was being sprayed with a fine mist of sea water.
I kept sail up as we passed through the narrow channel into the
'harbour' area of Kota Kinabalu and it was with some relief when I
anchored in the river off the Wawasan area of town. Roger, Jordan
and I went ashore to have a look around for another battery for my
laptop (mine only holds a charge for a few minutes now) but it seems
that one would have to be ordered from mainland Malaysia. Later, a
frantic phone call from Astrid sent us hurrying back to the boats - mine
was up against a fishing boat! Thoughts that my anchor had dragged
proved not to be the case, it was the fishing boats (three of them
rafted together) that had swung wide on their rope rode and had smacked
up against my port side. Astrid had the presence of mind to go
over to my boat and place fenders between the hulls which prevented any
damage. So, now, in the dark, we had to get my anchor up - and
that was underneath the fishing boats - and re-anchor some distance away
from them. On completion, we had a few drinks onboard until it was
time for bed.
19/11/11 With the engine now cool, I was
able to take off the exhaust elbow. We went around to Sutera
Marina to find out where the engineering area of town was, and while
Astrid and Jordan went shopping, Roger and I took a bus out to Inanam to
find Jesselton Engineering. The company has an extensive workshop,
open air but sheltered with a large corrugated iron roof, and they
firstly tried to weld up the hole (centre of photo) but as the casting is aluminium alloy,
the hole just got bigger and proved impossible to weld. A new one would
have to be made from 304 stainless steel as 316 marine grade steel is
almost impossible to get hold of. We then heard the sound of
heavy rain on the iron roof.......and we had a considerable walk to the bus
stop ahead of us! Kindly, one of the directors of the company said
he would take us back to town in his car, and that he would phone me on
Monday when he would have a price for a new exhaust elbow. He
warned us about our anchorage being unsafe because of the thieves in the
area - a fact we already knew about. Our intended one night stay
had once again been extended through no fault of our own.
20/11/11 Ashore again at noon to meet up
with Pete, Donna and kids (Orono) with whom Leah had been staying
since our arrival. After lunch together, they all went off to
ten-pin bowling while I had a wander around the shops. Some
shopkeepers said I may be able to get a battery for my laptop at
Karamunsing, but a later visit there proved fruitless - it would have to
be ordered, with a delivery time of Wednesday or Thursday - and the bus
conductor on the return journey was a rip-off merchant, overcharging
greatly, which angered me immensely. I don't like Kota Kinabalu!
There isn't even any mobile phone internet connection despite this being
the capital of Sabah.
21/11/11 I went by bus to Inanam and
spent an hour or so looking for the Toshiba Service Centre where I
ordered a new laptop battery to be delivered from Kuala Lumpur
22/11/11 A boring day doing practically
nothing except waiting around for parts! Roger paid a visit to the
Doctor's to get treatment for his painful foot - it seems he's been
bitten by something and it has now become infected. Henry joined
Storm Dodger as crew for a week or so. A late
afternoon call from Sue in the Toshiba Service Centre told me that my
battery had arrived in Inanam. Now that was a quick service!
23/11/11 Roger, the kids and Henry went
into town this morning while Astrid and I caught the bus to Inanam to
collect my laptop battery. We then returned to town and went to
the Doctor's because of a recurring hearing problem I have in my right
ear - he said I had a temperature and that the constriction of my throat
was causing the ear canal to close down as well. Anyway, I came
away with a bunch of antibiotics to take for the next week (6 tablets a
day......I'll rattle!) We then caught another bus out to
Karamunsing and wandered around the shops there until finally getting a
call from Jesselton Engineering saying my exhaust pipe would not be
ready until tomorrow. We then returned to the boats.
24/11/11 Again caught the bus to Inanam
and picked up my newly fabricated water injection exhaust elbow. I
don't know how long this will last but I will try to obtain another from
the UK as soon as possible. My main worry now is similar
to every car drivers problem - on a three section car exhaust, when you
replace one section the next in line usually fails shortly afterward!
That for me would be a huge problem as the next sections would be
totally inaccessible without first removing the engine, gearbox and
propeller shaft from the boat. Roger again went to the doctor
about his foot which is getting no better, in fact it's getting worse,
and he was referred to the hospital for further examination and
treatment.
25/11/11 Roger's foot problem is a
fungus with bacterial infection.....so the hospital say! Anyway,
he has more medication to take and potions to rub in. Today was a
bit of a rush, I fitted the water injection elbow at 6am this
morning, tested for leaks etc and then went ashore to do some shopping,
get some dinghy glue and exchange money for Filipino Pesos before coming
back to the boat, deflating and stowing the dinghy, putting shopping
away and generally tidying the boat for sea. We weighed anchor at
4pm and made the short trip out to Palau Gaya where Roger anchored on
the leeward side for the night, and I rafted up alongside.
26/11/11 Cast off around 0830 and made
our way around the western tip of the island before setting course in a
north-easterly direction. As the wind was either from the north or
north east, it was mostly motor sailing again but I did get some pure
sailing in as well, making reasonable progress in a later, rather lumpy sea.
The new exhaust elbow seems to be doing well, and as yet there are no
signs of any leaks from it. We arrived in the bay of Teluk Usucan
at 1600 and anchored in about 7 metres. It isn't a very
picturesque bay, there is a lot of road construction going on in the
small hamlet and only one other boat is anchored here. BBQ onboard
Storm Dodger in the evening. The photo is looking in a
general easterly direction over Pulau Sapangar toward Mount Nonohan in
the distance.
27/11/11 In the engine compartment early
this morning to change the gearbox oil in accordance with the manual
-change after the first 25 hours use (I've actually done 30 hours), then
breakfast and weigh anchor at 0900, making my way out of the bay and
again setting a course northward to White Rocks. Later on, we
changed our minds and altered course to go further out to sea and anchor
in the Mantanani Islands. Of course the wind backed northerly and
was right on our nose! Combined with a boisterous sea and 1.5
metre waves, the going was a little slow and it wasn't until 1445 that
we anchored off Pulau Mantanini Besar. Unfortunately, it's a rocky
bottom and I hate that........the sound of anchor chain dragging across
rocks all night!
28/11/11 As feared - an awful night of
anchor chain noises, scraping and banging as it dragged across the rocky
bottom, keeping me awake for the entire night. I guess I got about
an hour of sleep in total, made up of five or ten minute periods!
The morning didn't start off well either.....I weighed anchor at 0745,
and that was a struggle to get up. Then a few minutes later, as I
hoisted the mainsail, three-quarters of the way up, it jammed! The
main halyard was twisted around an unused bracket close to the mast
head, so I had to drop the sail again and circle downwind until it freed
itself. I then turned into wind again and hoisted the whole sail,
only to then find that the shackle connecting the boom and mainsheet had
parted, so I once again had to lower the sail. After fitting a new
shackle, I was finally able to hoist sail again and set my course
northward. Again the wind was on the nose (is this the
Mediterranean?) so even though the engine was still running, I had to
tack to make any forwards progress in the rough seas. At 1500 I
eventually dropped anchor again in the bay at Tiga Bangau - this time in
mud, and although some swell comes into the bay causing fairly big
surfing rollers on the beach, and the boat to roll somewhat, at least I
would get a decent sleep. When Storm Dodger anchored close
by, Roger went to bed feeling unwell, his foot is getting no better.
29/11/11 Away again at 0730 and by 0900
we were rounding the lighthouse on Pulau Kalampunian which marks the
northern tip of Borneo. Once again the wind was dead ahead and I
had to drop the sail and motor down the eastern coast to drop anchor in
Murudo Bay, Kudat just after 1300. The bay was, in the early
1800's, renown for pirate activities. Here we said our goodbyes to
Henry after his week of sailing with Roger and Astrid, as he was going
off to explore more of Borneo.
30/11/11 Went over to Storm Dodger
this morning to help Roger with a generator problem which involves
removal of the pulley on the front of the crankshaft. No matter
what we did, neither of us could get the securing bolt to move, and we
broke a torque wrench and bent a half inch steel bar in the trying.
We will have to make another, stronger tool to get the bolt undone.
Later went into town to draw money at the bank (a right
performance that was) and to get fresh bread
and although I nagged him to seek out the hospital about his foot (the
inflammation is spreading up his shin), we returned to the boats without
doing so.
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